well I found out that the bolts for the waste gate came loose again. But I am not sure that is where the leak is from. All I know is that if I look straight up at all the pipe from under the car the exhaust is coming straight down. So I think I will be pulling the turbo and wastegate again tomorrow to re-seal everything. Car sounds pretty good, the exhaust...
BrApple's Blog
well tonight I was finally able to install the intake tube and air filter. I had to trim alittle bit more from the fender area to fit the tube but all worked out. After that I was going to mount up the power steering cooler but I found that the bolts I bought which I thought where the same where not. So I just left it how I had it. After that I drove around...
well it took from 5 to about 8~8:30 but the wastegate exhaust leak has been corrected. To get the wastegate out I had to dissconnect the exhaust and remove the downpipe with the wastegate attached. Well to my frustration it wouldn't go back together that way. So back out it came and I also had to unbolt the turbo to get everything to line up. Again the...
well I kinda broke it already ....
that exhaust leak is at the wastegate. I thought I had it tightened down enough but I was wrong. That first time I really got on it the gasket on the up-pipe side blew out. I tightened then down more today but what was done was done. I was over excited to drive it. So my hope is that I can just pull the two bolts and...
that exhaust leak is at the wastegate. I thought I had it tightened down enough but I was wrong. That first time I really got on it the gasket on the up-pipe side blew out. I tightened then down more today but what was done was done. I was over excited to drive it. So my hope is that I can just pull the two bolts and...
so yet again another long day getting the turbo installed and up and running.
The morning started off with getting all of the hot side piping and turbo installed. By early afternoon that was completed. I then went about getting all of the charge pipes installed. Alot of the couplers needed to be cut down to make everything line up correctly. All in all...
The morning started off with getting all of the hot side piping and turbo installed. By early afternoon that was completed. I then went about getting all of the charge pipes installed. Alot of the couplers needed to be cut down to make everything line up correctly. All in all...
the correct tools ftw
I picked up a allen wrench socket set and some stubby wrenches and the plugs for the oil feed and drain came right off. I was able to reinstall just about all of the hot piping and the turbo. The turbo will need to come back out so once it is clocked correctly the flanges are tightened down. Once that is completed the oil drain will...
I picked up a allen wrench socket set and some stubby wrenches and the plugs for the oil feed and drain came right off. I was able to reinstall just about all of the hot piping and the turbo. The turbo will need to come back out so once it is clocked correctly the flanges are tightened down. Once that is completed the oil drain will...
I feel like I got my ass kicked today ...
I started off with a new tune from Joey. Everything was running right so on to the turbo install.
I was loaned a hole saw from some other guy at my storage unit, he was working on his car and snapped the allen wrench off in his coil over adjustment. Luckly the magnet I had was small enough to get the peice out....
I started off with a new tune from Joey. Everything was running right so on to the turbo install.
I was loaned a hole saw from some other guy at my storage unit, he was working on his car and snapped the allen wrench off in his coil over adjustment. Luckly the magnet I had was small enough to get the peice out....
getting closer
I was able to upgrade the fuel system today and tune the car. Everything was straight forward. The injectors and spark plugs where easy to swap. I was able to get it all done since I figured out an intake last night so that I can drive the car. I took one of the intake...
I was able to upgrade the fuel system today and tune the car. Everything was straight forward. The injectors and spark plugs where easy to swap. I was able to get it all done since I figured out an intake last night so that I can drive the car. I took one of the intake...
well now that Spring Zing is done and over I can get back to my turbo project. First up will be the fuel injectors and spark plugs. I have the 42# injectors and the NGK TR6 spark plugs to install. I will then either just make sure the car runs without any fuel leaks or I will try to get the 80mm maf installed so that I can tune the car and make sure it...
todays efforts in HDR ... one coat Z-AIO and one coat of Z5 applied and removed with the PC...
Recent Entries
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Done04 June 2008 -
98% complete29 May 2008 -
back on track28 May 2008 -
one problem27 May 2008 -
day two26 May 2008
Recent Comments
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day 1 continuedBy BrApple
May 29 2008 07:44 AM -
day 1 continuedBy Adam98SVT
May 26 2008 09:27 AM -
another weekend downBy BrApple
May 05 2008 07:23 PM



