well I found out that the bolts for the waste gate came loose again. But I am not sure that is where the leak is from. All I know is that if I look straight up at all the pipe from under the car the exhaust is coming straight down. So I think I will be pulling the turbo and wastegate again tomorrow to re-seal everything. Car sounds pretty good, the exhaust...
- Viewing Profile: Blog: BrApple
Community Stats
- Group Members
- Active Posts 1,514
- Profile Views 5,862
- Member Title Senior Member
- Age 30 years old
- Birthday August 25, 1981
-
Gender
Male
-
Location
Enfield, CT
Previous Fields
-
Vehicle owned
1999 Contour SeVT 3.0L Turbo
4
Neutral
User Tools
Blog Entries
BrApple's Blog > Done
Posted 04 June 2008
BrApple's Blog > 98% complete
Posted 29 May 2008
well tonight I was finally able to install the intake tube and air filter. I had to trim alittle bit more from the fender area to fit the tube but all worked out. After that I was going to mount up the power steering cooler but I found that the bolts I bought which I thought where the same where not. So I just left it how I had it. After that I drove around...
BrApple's Blog > back on track
Posted 28 May 2008
well it took from 5 to about 8~8:30 but the wastegate exhaust leak has been corrected. To get the wastegate out I had to dissconnect the exhaust and remove the downpipe with the wastegate attached. Well to my frustration it wouldn't go back together that way. So back out it came and I also had to unbolt the turbo to get everything to line up. Again the...
BrApple's Blog > one problem
Posted 27 May 2008
well I kinda broke it already ....
that exhaust leak is at the wastegate. I thought I had it tightened down enough but I was wrong. That first time I really got on it the gasket on the up-pipe side blew out. I tightened then down more today but what was done was done. I was over excited to drive it. So my hope is that I can just pull the two bolts and...
that exhaust leak is at the wastegate. I thought I had it tightened down enough but I was wrong. That first time I really got on it the gasket on the up-pipe side blew out. I tightened then down more today but what was done was done. I was over excited to drive it. So my hope is that I can just pull the two bolts and...
BrApple's Blog > day two
Posted 26 May 2008
so yet again another long day getting the turbo installed and up and running.
The morning started off with getting all of the hot side piping and turbo installed. By early afternoon that was completed. I then went about getting all of the charge pipes installed. Alot of the couplers needed to be cut down to make everything line up correctly. All in all...
The morning started off with getting all of the hot side piping and turbo installed. By early afternoon that was completed. I then went about getting all of the charge pipes installed. Alot of the couplers needed to be cut down to make everything line up correctly. All in all...
- Viewing Profile: Blog: BrApple
- Terms of Service




Find content